Harold Bawlzangya Racing

Modifications

What were they thinking?

Both Unitized Kawasaki rear ends I bought had bad input shaft bearings.  One rear end still rotated smoothly by hand, but the other was just shy of being locked up.

Guess which oil guide belonged to each rear end:

poorrearenddesign-7

Not sure how the designers/engineers thought any oil would get to this bearing!?  Oil guide blocking the bearing on one side:

poorrearenddesign-4

Governor sprocket on the other side:

poorrearenddesign-5

At least the other side has a little room for oil to get to the bearing.  The clutch side bearing of both rear ends was in much better shape.  I’m sure it was still out of spec, but it wasn’t obvious to the naked eye.

poorrearenddesign-1

This is the governor side bearing from the rear end that was toast.  The inner race shouldn’t be able to do that.

poorrearenddesign-8

When that happens, things start rubbing that shouldn’t:

poorrearenddesign-9

So Club Car’s solution to this bad design are sealed bearings:

poorrearenddesign-11

I’m going trust this over what was used from the factory:

grease

Being very careful, got the seals removed:

poorrearenddesign-12

Grease in the other bearing:

poorrearenddesign-13

Got all the grease out and ready for the red stuff:

poorrearenddesign-15

I know you can over-pack a bearing with grease, but I figured that they used the bare minimum at the factory.  With the factory grease being dark in color, it was a little tough to gauge just how much was in there.  So I tried to add as much as I could while still allowing some room for extra grease to move into as the bearing got some use.

poorrearenddesign-17

Time will tell how well this holds up.


One EXP conversion done, working on two more

The parts needed to make a few Rekluse conversions:

expparts

One is done and out the door today.  Just waiting on a few parts to finish the others.

conversionoutthedoor


2016 Summer Project – 1992 Gas Club Car build

Bought this in June 2016.  This is part of the reason I didn’t do any riding over the summer.  That and it was really stinkin’ hot.  Most of my time and all free money went towards this project.

1992clubcar

Tear down:

clubcardisassembly-3

clubcardisassembly-2

clubcardisassembly-1

clubcardisassembly-4

engineremoved

24 years of oil, dirt, grass and twigs:

gunk

old290

New engine:

new290

Machined driven clutch and 8:1 gears:

machinedclutch8-1gears

rearend

The kids have been driving this to school for a couple of months now.  With the 8:1 gears, it will do about 22-23 MPH at around 3,000 RPM.  The engine could run safely at 4,000 RPM, but teenagers don’t need to be going that fast on most of the paths.

finishedgascc-2

finishedgascc-1


NoToil comparison

After using the FilGuard filter I bought a while ago, I wasn’t that impressed.  But to be fair it was exceptionally dusty and the dust was so fine that it lingered in the air a long time.

Back when I did my air filter test, the NoToil filter performed very well.  Thinking that all NoToil filters where the same, I ordered one of the pre-oiled ones:

notoilcomparison-10

Right out of the bag I was surprised:

notoilcomparison-5

Years ago I used NoToil oil but had oil settle to the bottom of the filter and drip in the airbox.  I thought it was just be over-oiling, but I read complaints from others as well.  I stopped using it.  I am certain the machine that applies the oil in the factory is putting on the bare minimum, so I wasn’t expecting to see it settle out in the bag.

notoilcomparison-13

Without opening the inner bag, the filter material itself looked different than the one I tested years ago:

notoilcomparison-12

I went into the other room and turned the desklamp over:

notoilcomparison-6

I wasn’t liking what I was seeing:

notoilcomparison-15

I called RockyMountain up and got my return authorization for the pre-oiled filters I bought.  A quick check on eBay and I found a non-oiled NoToil filter.  A few days later this is what I received:

notoilcomparison-9

notoilcomparison-11

A quick side-by-side and you can easily tell that the foam isn’t the same between the two:

notoilcomparison-17

Nothing special about the sealing surface like on the Moose filters:

notoilcomparison-1

Now this is what I was looking for:

notoilcomparison-8

Seems like you give up quite a bit for the convenience of not having to oil the filter.


Image

First of several Rekluse EXP modifications

ClutchMods (1)

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Letting the oil flow

As I’m putting the 220 together, this was a good time to modify the clutch hub I have been using.  One of the used YZ clutches I bought a while ago came with a Hinson hub.  That hub had a lot of big oil holes in it:

YZHub

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The stock hub has 4 small holes:

HubOilHolesBefore

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So without going too crazy, I went from 4 small holes to 16 larger ones:

HubOilsHolesAfter

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That is more like it

220CylinderHead (1)

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Looks like I won’t be needing to hand-cut any gaskets for a little while now:

220TopEndGaskets

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HBR-CSRS #392 installed

More pictures HERE:

 

220CrankSeals (5)

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220CrankSeals (8)

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220CrankSeals (4)

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220CrankSeals (9)

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220CrankSeals (11)

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220CrankSeals (2)

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GovernorClearance

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Cleaning the KIPS

I had some of this cleaner that I was looking to get rid of so I thought I would try it on the KIPS parts.  Started soaking just this part:

CleaningKIPS (3)

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Then added some more and let them sit overnight.  It got off a lot of the gunk,

CleaningKIPS

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but it didn’t get all of the heavy carbon build-up:

CleaningKIPS (4)

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CleaningKIPS (5)

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CleaningKIPS (8)

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CleaningKIPS (9)

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I went to a fine wire wheel and had to work to get this stuff off:

CleaningKIPS (10)

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Soaked the rest of the KIPS in more of the combustion cleaner and they came out pretty clean:

CleaningKIPS (6)

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CleaningKIPS (7)

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In time we’ll see how well the carbon does/doesn’t stick to the more polished surfaces.  If I was going to polish this correctly, I would have had to have sanded out more of the metal to get rid of the imperfections for a nice surface.  But I didn’t want to remove metal and screw with the tolerances of the parts.  So all of the polishing was done with a buffing wheel.  Not a mirror finish, but it should be a bit “slipperier” than it was before:

PolishedKIPS (1)

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PolishedKIPS (2)

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A final clean-up in acetone and all ready to install:

CleaningKIPS (1)

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220 KIPS bore clean-up

It is not uncommon for some excess plating to buildup inside the bore of the KIPS system when the cylinder gets replated.  The left side isn’t a problem, but the right side that uses the o-ring on the exhaust rod can cause binding.  Removing the o-ring is not the proper fix.

I kept the old o-ring on and tested the cylinder to see how much resistance was on the rod.  I didn’t want to tear up the new o-ring.

220borecleanup (2)

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Not too bad, but it could be better.  Featuring the HBR Power Valve Bore Resurfacer, or HBR-PVBR for short.  Made from the highest quality materials, machined to the tightest of tolerances:

220borecleanup (3)

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I started with some 320 grit wet/dry sandpaper:

220borecleanup (4)

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220borecleanup (6)

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220borecleanup (5)

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220borecleanup (1)

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I moved the HBR-PVBR in and out of the bore several times while running the drill.  I checked the exhaust rod for proper operation.  I finished the process with 400 grit wet/dry sandpaper.   The rod moves smoothly with no hang-ups or unnecessary resistance.

 


Got the bottom end of the 220 put together

More pictures and details HERE.

casecleaning (1)

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220BottomEnd4

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220BottomEnd5

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220BottomEnd6

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200BottomEnd10

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220BottomEnd12

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220BottomEnd14

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220BottomEnd21

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220BottomEnd20

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220BottomEnd25

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220BottomEnd27

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220BottomEnd29

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220BottomEnd35

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220BottomEnd36

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220BottomEnd37

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220BottomEnd38

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220BottomEnd40

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220BottomEnd41

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220BottomEnd42

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Soda blasting cases

With all the modifications done to the cases, it is time to clean them up.   The Harbor Freight soda blaster works surprising well.

Soda blasting (2)

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Soda blasting (8)

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Soda blasting (6)

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Soda blasting (5)

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Soda blasting (4)

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Done with the soda,

Soda blasting (7)

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Soaking in hot, Dawn filled water to get rid of all the baking soda:

Soda blasting (1)

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Well I thought soaking them for a while and then using the handheld sink sprayer would have dissolved/removed all the baking soda.  But after speed drying the cases in the oven, I was wrong.  There was still baking soda in some of the blind bolt holes.

casecleaning (2)

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casecleaning (3)

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So back to the utility sink. This time I bought a tooth pick and poked it around in all the bolt holes while spraying it with the handheld sprayer.  Speed drying in the oven again and finally the cases are clean.

casecleaning (1)

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Final truing of the HBR crank

I’ve had this crank I rebuilt a while ago stored away waiting for a bottom end to put in.  I thought I’d check the run-out one last time before I installed it.  It was well under specs, but I thought I’d push my luck and see if I could get it better.

I put the indicators as far out as possible to get the best reading.

finalcranktrue (5)

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Kawasaki didn’t make it very easy on the clutch side.  Between the keyway slot and the locator pin hole for the water pump gear, there isn’t much real estate to work with:

finalcranktrue (6)

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The flywheel side didn’t have as many obstacles, but with the taper, any later movement would throw the reading off:

finalcranktrue (7)

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After just a handful of calculated whacks, I had the indicator on the flywheel side just barely moving and the clutch side was just under .001″ out.

I didn’t set-up the indicators exactly like outlined in the manual, but this orientation should highlight the run-out a little better than what is shown in the manual.

finalcranktrue (1)

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Both indicators barely moved.  Even with the limitations of my set-up and indicators, this should be a long lasting and smooth running crank.


Image

Not too shabby

IntakeAfterPlating

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HBR – Crank Seal Retainer System (patent pending) Model 392

Logic told me that the crank seals weren’t going to blow out of the cases with the retaining lip removed.  But I had the time, material and paranoia to try to add some peace of mind to this modification.  Born is the HBR-CSRS model 392.

For the clutch side, I used some acrylic to mock-up what the retainer would look like:

plasticprototype

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Originally I was going to use 1/2″ aluminum and machine away most of it for the necessary clearances.  I wouldn’t have to bend anything and the differences between where the retainer bolted to the cases and where it rested against the seal would be easy enough to work out.

halfinchprototype

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But I took a quick stab at making one out of thinner aluminum and seeing if I could get the bends correct.  I think it was more luck than anything but I got this worked out:

FinalVersion

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I added this drain channel to the backside.  This isn’t so much for oil to drain out but rather to give the sediment from the worn clutch friction material a place to drain away. It just seems like a bad idea to have that abrasive material collecting near the crank seal.

ClutchSideRetainer-Channel

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Other than removing the factory cast retaining lips,

RetainerClutchSideBefore (1)

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I put this notch in the alignment dowel part of the case:

RetainerClutchSideBefore (2)

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The retainer fits into this notch,

RetainerClutchSideInstalled (1)

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And then bolts into place on top of the existing oil receiver:

RetainerClutchSideInstalled (2)

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Inside view:

RetainerClutchBackside

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Flywheel side was a little easier. Using a spare, I removed the electronics and started with this:

FlywheelSealRetainer (2)

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Put it on the scanner and cut out a template:

RetainerFlywheelSideTemplate

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RetainerFlywheelSideTraceOut (2)

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RetainerFlywheelSideTraceOut (1)

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After some work I had this:

FlywheelRetainer (2)

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FlywheelRetainer (1)

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Ready to bolt on:

RetainerFlywheelSideInstalled (3)

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RetainerFlywheelSideInstalled (4)

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With the retaining lip removed:

RetainerFlywheelSideInstalled (2)

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Installed:

RetainerFlywheelSideInstalled (5)

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RetainerFlywheelSideInstalled (1)

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Now I’ve got the peace of mind that the seals won’t push out, yet with the removal of a few bolts I can still service them.

 

 


What are those?

 

FinalVersion

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FlywheelRetainer (1)

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FlywheelRetainer (2)

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Splitting the Rekluse EXP test engine

With the last EXP conversion shipped out, I thought I’d take a few minutes and split the engine I used to test fit the conversions on.   I think I used this on 15 conversions:

TestEngineSplit (2)

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So here we go, getting the flywheel off:

TestEngineSplit (3)

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TestEngineSplit (4)

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TestEngineSplit (5)

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Before you start trying to split the cases, double-check that you have removed 11 case bolts:

TestEngineSplit (6)

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As usual, a nice “pop” that makes you think you just broke something:

TestEngineSplit (7)

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One I get the “pop” and initial separation at the crank side of the cases, I start tapping the rear of the cases with a rubber mallet to get them separated.

TestEngineSplit (8)

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Separating and tapping a little at a time making sure gap stays consistent between the front and rear of the cases:

TestEngineSplit (9)

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Just about there:

TestEngineSplit (10)

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TestEngineSplit (11)

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Got lucky on this one that both crank bearings stayed in the cases.  Usually one stays on the crank.

TestEngineSplit (12)

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Cylinder arrived today

My 220 cylinder came back from PowerSeal today.

I shipped it off on December 30th (Wednesday).

It was delivered on January 2nd (Saturday).

Received an email from them on January 4th (Monday) letting me know they received the cylinder – nice touch.  Emailed stated that turnaround time was currently 9 days.

Received a call on January 11th (Monday) that the cylinder was done.  $207 shipped back to me.

Cylinder was delivered on January 13th (Wednesday).

They send it back in the same box with the same packing you shipped it in.

PowerSealRePlate (4)

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PowerSealRePlate (5)

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PowerSealRePlate (8)

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PowerSealRePlate (7)

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PowerSealRePlate (6)

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PowerSealRePlate (1)

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PowerSealRePlate (3)

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PowerSealRePlate (2)

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Case modification – replace crank seals without splitting the cases

Better way HERE.


 

I’ve been researching this for a while and finally took the plunge.  Yamaha and Honda allow you to replace the crank seals without splitting the cases.  But these lips that Kawasaki manufactured into the cases prevents that.

Partial lip on flywheel side:

Cases - crank seal removal (10)

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Cases - crank seal removal (4)

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Full lip on clutch side:

Cases - crank seal removal (2)

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Cases - crank seal removal (3)

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Honda doesn’t use a retainer on either crank seal:

http://www.allthingsmoto.com/forums/f-235/round-three-92-01-cr250-engine-build-46010/

 

And Yamaha only uses a retainer on the clutch side (~5:20).   At about 5:46 of this video, he just pushes the crank seal in with his fingers.  I can’t tell from any of the 3 RMATV videos, but the stator could serve as a seal retainer.  But I did notice that the seals Yamaha uses are different than what the KDX uses.  No way are you installing the KDX seals with just your fingers.

 

The more I’ve thought about it, I’m thinking those “lips” are more of stops that put the crank seal in the correct location.  If there was concern about the seals moving and popping out, I would think there would be an equal concern with the seals moving inwards and blocking off the oil passage.  I’ve yet to see a seal that wasn’t seated against the lip, so I highly doubt that they move.

So here we go . . .

Flywheel side removed:

Cases - crank seal removal (12)

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Clutch side removed:

Cases - crank seal removal (15)

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Neat little drill bit

I bought this drill bit a while ago from eBay.  It was made in Poland and didn’t cost that much.  I wasn’t sure how it would work out and I finally have a chance to try it out on my 220 build.

The first part is a 15mm guide and the cutting part of the bit is 17mm.

drillbiit (2)

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drillbiit (1)

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HybridCasesShavings

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Worked very well:

HybridCasesSecondCut

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HybridCasesDone2

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Blind bearing removal – no puller required

You don’t need too much to get the blind bearings out of the cases.  What you are trying to do is to force a material back behind the bearing so it applies pressure to the bearing to push it out.

I was fortunate enough to have some leftover parts that I could use to get the bearings out.  You could use anything as long as it fits tightly within the inner race of the bearing.  You don’t want the material you are using to escape between the inner race and whatever you are using to force the material back behind the bearing.

BlindBearingRemovalTools

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I use plumbers putty:

PlumberPutty

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And some heavy duty packing paper.  Newspaper can work OK, but when you wet it down, it tends to disintegrate much easier than this brown packing paper.

BlindBearingRemoval-Paper (10)

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The transmission bearing:  For this one I use plumbers putty, it makes quick work of removing the bearing. Fill the bearing up:

TransmissionBlindBearing (1)

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Then hammer it in:

TransmissionBlindBearing (2)

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Keep repeating that process of adding more putty and hammering it in until the bearing starts to lift out:

TransmissionBlindBearing (3)

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TransmissionBlindBearing (8)

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TransmissionBlindBearing (9)

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TransmissionBlindBearing (12)

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TransmissionBlindBearing (13)

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TransmissionBlindBearing (15)

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TransmissionBlindBearing (16)

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TransmissionBlindBearing (17)

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Water pump bearing:  I did a little experiment here, I used a combination of the brown paper(dry) and plumbers putty.  It is a little difficult to see, but I’ve packed some of the dry brown paper down into the bearing.  This is to try to keep the plumbers putty from getting forced up through the openings in the bearings.

BlindBearingRemoval-Paper-PlumberPutty (4)

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Add some putty:

BlindBearingRemoval-Paper-PlumberPutty (5)

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Hammer it in and keep repeating:

BlindBearingRemoval-Paper-PlumberPutty (6)

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BlindBearingRemoval-Paper-PlumberPutty (7)

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BlindBearingRemoval-Paper-PlumberPutty (8)

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The leftover mess:

BlindBearingRemoval-Paper-PlumberPutty (9)

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 BlindBearingRemoval-Paper-PlumberPutty (10)

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The KIPS governor bearing:  I’m using just the wet brown packing paper on this.  Same approach as the other bearings.

BlindBearingRemoval-Paper (1)

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BlindBearingRemoval-Paper (2)

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BlindBearingRemoval-Paper (4)

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BlindBearingRemoval-Paper (6)

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BlindBearingRemoval-Paper (9)

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Got a little carried away with the case sealant

How it came from the factory:

ExcessCaseSealant (6)

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ExcessCaseSealant (7)

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Crank Rebuild

My first attempt at rebuilding a two stroke crank.  I’m starting with this H-series KDX crank:

CrankRebuild (3)

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A few minutes with a fresh cut-off wheel on the angle grinder:

CrankRebuild (4)

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Remember to press the crank pin from the outside-to-inside.  You don’t want to press the crank pin out so the cut portion has to pass through the crank web:

CrankRebuild (5)

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Using a Pro-X (OEM) crank rebuild kit.  $58 on Amazon:

CrankRebuild (6)

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First step installing the crank pin:

CrankRebuild (7)

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CrankRebuild (8)

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Bearing and washers on:

CrankRebuild (9)

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Because I don’t have a nice jig that ensures nearly perfect alignment like the crank builders do, I pressed the other crank web on in steps.  Once I got it started, I put in on the v-blocks and made adjustments to get the run-out below .001″.  Because the crank pin wasn’t fully seated, these adjustments took very little force. I repeated this partial press/adjustment process a total of three times.  This is what the crank looked like after the 3rd press:

CrankRebuild (10)

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Final press:

CrankRebuild (11)

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Specs on side clearance:

CrankRebuild (2)

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CrankRebuild (13)

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CrankRebuild (12)

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A quick video showing my run-out during part of the process:

 


Back to the KX250 silencer

I am going to go back to the KX250 silencer, for a while at least.

First step is adding the spacer, like I did HERE.  This time I am going to go with aluminum.

KX250Silencer (1)

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I had to pry it apart just to get it started:

KX250Silencer (2)

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Then tapped it on the rest of the way:

KX250Silencer (3)

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KX250Silencer (5)

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KX250Silencer (6)

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Ready to go:

KX250Silencer (9)

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